FPV Quadcopter Build Update

Well… My first quadcopter build that I’ve, for some reason, named the Gecko, isn’t coming along well. But it will come as soon as it actually works right. A list of problems:

1. It doesn’t fly for more than 3 minutes.

2. Something happened (a sudden increase in current draw from motors?) that caused it to lose power and crash. I replaced motors to slightly slower ones, but I haven’t pushed it as far as I did when it crashed yet. 

3. Even with short flight times, it uses a 700-800 mAH battery.


I am currently trying to fix these problems so I can post a build guid soon. Thanks for reading umFlight!